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Thread: Sticky Float - Adjust the plastic float?

  1. #1
    Join Date
    Feb 2006
    Location
    Central Florida
    --
    1,090

    Sticky Float - Adjust the plastic float?

    How do I adjust the float level if the float is 100% plastic? My two brain cells have argued about it long enough........

    The 250es carb bowl is getting too full and it drips out the overflow - the carb is clean with a new kit in it. Now what?

    Here are a couple nice reads... does'nt help me much tho. Should I just try a different float?

    http://www.factorypro.com/tech_tunin...procedure.html

    http://www.xs11.com/tips/maintenance/maint20.shtml

    anyone ever do this clear tube trick to see how high the fuel is?
    quiet people seem intelligent

  2. #2
    Join Date
    Sep 2005
    Location
    Lipetsk, Russia
    --
    2,824
    If you've got a sticky float, try replacing the pin that holds it in the carb (those two prongs). Mine was slightly tweaked on my 125 carb and I replaced it with a slightly undersized nail, and it worked just fine.
    I'm back in the USSR...

  3. #3
    Join Date
    Apr 2006
    Location
    Crestview, Florida
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    2,429
    its prolly the needle valve.

  4. #4
    Join Date
    Jul 2006
    Location
    western ny
    --
    3,366
    as jeswinehart said... i would clean the hell out of that pin. them plastic floats can not be adjusted. while your cleaning the pin make sure the float seat isnt sticking as well.
    down to parts because i no longer have a place to ride trikes.

    GIT IT RAAAGGGGG !!!!

  5. #5
    Join Date
    Mar 2006
    Location
    PA
    --
    3,515
    with carefull heat they can be ajusted.... but they break very easy as well
    80s......185 atc, Yamaha tri-moto 200, 85 200x with tons of work
    90s......89 Suzuki quad racer 250 (raced 250 A class for 6 years, late 90s.. custom framed 250x with long travel shocks and a built 350x motor.... built Honda 110
    00s...... chomeoly framed 350 RX with all the goodies (thanks to my bro)
    2012.....Replaced the 350x motor for a 444cc YZ426
    WWW.HREATV.COM

  6. #6
    Join Date
    Feb 2006
    Location
    Central Florida
    --
    1,090
    hmmm... the float seemed to operate good when I had it apart. I will break it down and try two things; I will polish the pin out good and switch floats in case that one has a hole in it - how could it be the needle valve? are you talking about the float jet that the rubbber tipped float needle sits in?

    I should have a handful of those pivot pins that the float rides on so I will swap it too....

    let me know how it could be the needle - I have already had it off once and don't want to keep removing it

    thanks
    quiet people seem intelligent

  7. #7
    Join Date
    Mar 2006
    Location
    PA
    --
    3,515
    neddle valve = float jet
    80s......185 atc, Yamaha tri-moto 200, 85 200x with tons of work
    90s......89 Suzuki quad racer 250 (raced 250 A class for 6 years, late 90s.. custom framed 250x with long travel shocks and a built 350x motor.... built Honda 110
    00s...... chomeoly framed 350 RX with all the goodies (thanks to my bro)
    2012.....Replaced the 350x motor for a 444cc YZ426
    WWW.HREATV.COM

  8. #8
    Join Date
    Oct 2007
    Location
    Grosse Tete, LA
    --
    3,440
    i had the same problem on my 200x...i bought a new float which came with a new pin... the pin is what fixed it.

  9. #9
    Join Date
    Feb 2006
    Location
    Central Florida
    --
    1,090
    Gracias Goat

    Swigo, what am I looking for on the needle jet? Anyone?
    quiet people seem intelligent

  10. #10
    Join Date
    Sep 2005
    Location
    Lipetsk, Russia
    --
    2,824
    Just general debris and crap. Clean it out real well, then play around with the float while blowing into the fuel line. If it leaks air with the needle closed, you need a new seat.
    I'm back in the USSR...

  11. #11
    Join Date
    Feb 2006
    Location
    Central Florida
    --
    1,090
    blow job, eh? ok - will give it a try and see what I can figure out. I have a different carb I can rob the seat from if needed.


    I will probably rubber band a clear drain hose to the carb so I can see where the float level is too.
    quiet people seem intelligent

  12. #12
    Join Date
    Nov 2006
    Location
    Tulare, California
    --
    719
    I am sure you put the float on and held the carb sideways and pushed the float in and out like the bowl is filling up and feel for hesitation? That round plastic skirt that sits on the main jet post under the float is on right?
    Current Bike:
    1985 Honda 350X

    Bikes owned:
    1984 Honda 200X
    1982 Honda 250R
    1985 Honda 350X x3
    1985 Honda 250R x2
    1985 Honda 500X

  13. #13
    Join Date
    Feb 2006
    Location
    Central Florida
    --
    1,090
    It is almost like I was in DENIAL that there could be any trash in the carb since I just cleaned the carb the other day.....

    RRAK, I blew through the fuel hose and could detect a very slight leak at the float jet - kind of perplexed, I broke it down and blew real hard in the the hose and it shot the chunk out.

    Thanks for the help!
    quiet people seem intelligent

  14. #14
    Join Date
    Sep 2005
    Location
    Lipetsk, Russia
    --
    2,824
    No problemo senor. That's one of the things that kept going wrong on my little 110 back when I had it, the tank was uber rusty and the needle valve kept leaking.

    I highly suggest an inline filter. That'll keep crap from being rubbed in the needle seat and wearing it out.
    I'm back in the USSR...

  15. #15
    Join Date
    Feb 2006
    Location
    Central Florida
    --
    1,090
    I removed the tank and repaired the rust in the bottom of it. When I pulled the outlet filter out of the tank it fell apart. When I cleaned out the petcock I got a teaspoon of sawdust looking rust bits. All clean, everything was installed with an inline filter.


    The junk that was in there was like a big booger. It was there before I soaked the carb and when I blew all the jets out the first time. I am really surprised It did not come one the first go round. The hard starting condition and the overflow problem were why I went thru the carb tho - I guess I just went thru the motions instead of focusing on the problem.
    quiet people seem intelligent

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