boosted96cobra
02-28-2010, 09:24 PM
Picked this bike up a couple weeks ago. Had a really bad top end tick.
Getting it home:
http://i291.photobucket.com/albums/ll292/sagep11/firstday.jpg
Got it in the garage and torn down, the tick was from this:
http://i291.photobucket.com/albums/ll292/sagep11/IMAG0295.jpg
Everything else motor wise looked in great shape!:
http://i291.photobucket.com/albums/ll292/sagep11/IMAG0293.jpg
http://i291.photobucket.com/albums/ll292/sagep11/IMAG0294.jpg
I wanted a bit more snap, so I upped the compression to a wiseco 10.25:1 comp piston (stock 81mm bore):
http://i291.photobucket.com/albums/ll292/sagep11/piston2.jpg
http://i291.photobucket.com/albums/ll292/sagep11/piston.jpg
Powroll small bore cam:
http://i291.photobucket.com/albums/ll292/sagep11/350xcam.jpg
New Honda oem rockers:
http://i291.photobucket.com/albums/ll292/sagep11/rockers.jpg
Ported head:
http://i291.photobucket.com/albums/ll292/sagep11/head.jpg
I also snagged a Supertrapp exhaust from Kasey.
The plastic wear cracked pretty bad, so I dune cut them. I still need to fix a crack on the right side:
http://i291.photobucket.com/albums/ll292/sagep11/IMAG0338.jpg
http://i291.photobucket.com/albums/ll292/sagep11/IMAG0342.jpg
I took it out to the dunes on friday. I had messed with the jetting a bit at home. It was stock at 138, I upped to a 140. With that is went to a point in the rpm range and just stopped, like it hit a wall. I upped it 1 size and it started to cut out. I took the rocker cover off to see if the cam was on, which it was. I re adjusted the valves and took it to the dunes.
At the dunes i went up a jet size and it started getting better. The plug was reading ok and decent power around a 150 main. It only really had low end and some mid range, no top end really.
After each stop riding, I kept jetting up. I finally ended up having it a hair rich at a 162!!! WTF? I think it would be good at a 160, of course those are the only size I didn't have, the Tecate and 250r both like around a 160 main.
I also took some time and lowered the rear and softened the setting on the rear shock. So far it is a decent ride.
It has a rack welded on the grab bar which I do really like. I am also having an issue with the lights. I have one right low than works, left nothing, on high neither work.
http://i291.photobucket.com/albums/ll292/sagep11/IMAG0340.jpg
http://i291.photobucket.com/albums/ll292/sagep11/IMAG0345.jpg
Getting it home:
http://i291.photobucket.com/albums/ll292/sagep11/firstday.jpg
Got it in the garage and torn down, the tick was from this:
http://i291.photobucket.com/albums/ll292/sagep11/IMAG0295.jpg
Everything else motor wise looked in great shape!:
http://i291.photobucket.com/albums/ll292/sagep11/IMAG0293.jpg
http://i291.photobucket.com/albums/ll292/sagep11/IMAG0294.jpg
I wanted a bit more snap, so I upped the compression to a wiseco 10.25:1 comp piston (stock 81mm bore):
http://i291.photobucket.com/albums/ll292/sagep11/piston2.jpg
http://i291.photobucket.com/albums/ll292/sagep11/piston.jpg
Powroll small bore cam:
http://i291.photobucket.com/albums/ll292/sagep11/350xcam.jpg
New Honda oem rockers:
http://i291.photobucket.com/albums/ll292/sagep11/rockers.jpg
Ported head:
http://i291.photobucket.com/albums/ll292/sagep11/head.jpg
I also snagged a Supertrapp exhaust from Kasey.
The plastic wear cracked pretty bad, so I dune cut them. I still need to fix a crack on the right side:
http://i291.photobucket.com/albums/ll292/sagep11/IMAG0338.jpg
http://i291.photobucket.com/albums/ll292/sagep11/IMAG0342.jpg
I took it out to the dunes on friday. I had messed with the jetting a bit at home. It was stock at 138, I upped to a 140. With that is went to a point in the rpm range and just stopped, like it hit a wall. I upped it 1 size and it started to cut out. I took the rocker cover off to see if the cam was on, which it was. I re adjusted the valves and took it to the dunes.
At the dunes i went up a jet size and it started getting better. The plug was reading ok and decent power around a 150 main. It only really had low end and some mid range, no top end really.
After each stop riding, I kept jetting up. I finally ended up having it a hair rich at a 162!!! WTF? I think it would be good at a 160, of course those are the only size I didn't have, the Tecate and 250r both like around a 160 main.
I also took some time and lowered the rear and softened the setting on the rear shock. So far it is a decent ride.
It has a rack welded on the grab bar which I do really like. I am also having an issue with the lights. I have one right low than works, left nothing, on high neither work.
http://i291.photobucket.com/albums/ll292/sagep11/IMAG0340.jpg
http://i291.photobucket.com/albums/ll292/sagep11/IMAG0345.jpg